So I bit the bullet and decided to replace the carby at last with a brand new 32/36 DGV.
interesting to see the clean and dirty sides of the intake
all installed, using stock full length cable, with some special engineering on the big washers on either side of the throttle bracket. stock rocker cover back on.
because this a factory manual choke carby, it works 10000000000000 x better than my converted manual choke carby, that used to be auto choke.
I got it running and driving, but couldnt use full throttle. would completely bog down and just die under load. So tonight, i pulled the top off carby to see why....
and this is what i found. yep, brand new weber, which i picked up myself from weber performance, and this is what i find. secondary main jet out, primary main jet was lose, just sitting in.
put them back, and got the car going and driving way way better, but still not 100%. im guessing its over jetted for the 1300.
this is the jetting comparison.
should make sense hopefully. the Renault Carby is what ive been running.